

Engine (26%)
Transmission and Drivetrain (8%)
Brakes and Traction Control (6%)
Suspension and Steering (17%)
Electrical and Air Conditioning (29%)
Paint, Rust, Leaks, Rattles, and Trim (10%)
Other (3%)
$2500+ (3%)
$1000 - $2499 (3%)
$500 - $999 (14%)
$100 - $499 (28%)
< $100 (53%)
Engine not specified
106000 mi US $550 |
Fuel delivery problem |
300-horsepower 4.6L V8 5-speed manual RWD
94000 mi US $400 |
VCT Sensor 2 |
24800 mi C $41 |
Faulty fuel cap causing PO456 check engine light |
46000 mi US $500 |
Rear differential service. |
9000 mi | Throttle cut out when accelerating - intermittent. Fuel pumps replaced. |
181961 mi US $570 |
Head gasket leak successfully sealed with K-Seal. Replaced thermostat. Camera viewing of cylinders to verify presence of coolant in combustion chambers in two cylinders. |
11780 mi | Car would not idle smoothly anymore. |
176000 mi US $955 |
Variable cam timing problem. Oil Control Solenoids, or phasers, or cam tensioner. No codes thrown, symptoms very mild, couldn't narrow it down. |
300-horsepower 4.6L V8 5-speed automatic RWD
20000 mi | Fuel pump and fuel level sensor replaced under warranty. |
81000 mi US $497 |
Replaced radiator. Radiator had small leak at join between plastic side and aluminum core. Seepage, really. Fluid loss was about 1 qt per 3000 miles. |
210-horsepower 4.0L V6 5-speed automatic RWD
55722 mi US $502 |
Check Engine light came on saying Short in Transmission Shift Solenoid. Dealer checked it and determined that there was a coolant leak around the thermostat housing that was causing it to throw a false code. |
135000 mi US $200 |
Car began to overheat and leaked coolant. Found that the water pump was leaking through the bearing weep hole. Replaced water pump, thermostat housing and accessory drive belt. |
138800 mi US $250 |
Replaced water pump and thermostat housing. |
167000 mi US $1200 |
Replaced thermostat and housing |
89000 mi US $18 |
engine light warning, was bad gasket on fuel filler cap. Replaced cap all ok |
28000 mi US $50 |
Fuel tank replaced to correct complaint that gas pump shuts off repeatedly while fueling even at very slow pace. |
49000 mi US $180 |
Car would lurch and make noise with loss of power for a brief moment and would then regain and be fine. Never stalled and had no loss of control. Problem was determined to be throttle sensor being dirty. Removed & cleaned throttle body & re-pgm. |
58000 mi US $50 |
Thermostat housing leak. Coolant had been leaking all over and was low. Replaced seal and housing parts. Drained coolant and replaced coolant (after a flush-maint item). |
88300 mi | Cracked Serpentine belt. |
90000 mi US $70 |
Replaced serpentine belt. Replaced radiator reserve cap. Car was running hot while idling. (Maint. work also elected: Decided to do coolant flush which was previously recommended and would help maintain cooler vehicle). |
105600 mi | Check Engine light came on. Examination revealed small leak in fuel line. Did not fix due to cost and cel reset itself. Issue only occurred once. |
177000 mi | It had an oil leak, sipped some coolant and had an occasional undiagnosed squeal from the engine compartment. |
87000 mi US $58 |
Replaced cooling manifold. Easy repair, houses the temp sensor. |
104000 mi US $100 |
Thermostat housing is plastic, glued together at the factory. Split and blew apart. |
104000 mi US $75 |
Coolant reservoir is a 2 piece plastic part, glued together at the factory. Seal broke resulting in loss of coolant. Replaced the tank. Coolant reservoir is a 2 piece plastic part, glued together at the factory. Seal broke resulting in loss of coolant. Replaced the tank. |
300-horsepower 4.6L V8 5-speed automatic RWD
47000 mi US $80 |
Vibration at 1200rpm TSB performed by Ford |
210-horsepower 4.0L V6 5-speed automatic RWD
31000 mi | Throttle position Sensor failure. TPS replaced. |
54000 mi US $300 |
Leaking coolant due to a cracked thermostat housing. |
49000 mi US $450 |
Check engine light was coming on. Replaced failed bank two HEGO sensor, reset PCM. Also replaced fuel filter and regular oil change. |
78200 mi | Right muffler pipe detached and rotted where the new dual exhaust system was put on. It needed to be re-welded. |
96000 mi US $3200 |
replaced: LT valve cvr, valve cvr gasket, Lt timing case, tensioner, seal assembly, water pump/gasket, R&I oil pan, debris from engine/pan, flush coolant, antifreeze |
96000 mi | An "O" ring broke from a previous repair in September. The shop repaired the ring and did another oil change. The car had less than 50 miles between oil changes, but it needed to be done. She is running great at this time. |
100000 mi US $250 |
R/S of Pypes dual exhaust pipe shifted to the right. Mechanic re-positioned, but the clamp cannot be tightened any further. Re-positioned CAI for rattle. |